Has it really been 5 months since my last update? There’s been a lot of activity, unfortunately quite a bit of it resulting in dead ends. But I’m back on track now. Here’s a brief summary of what went on.
After priming the interior I set out to repair the collision damage to the rear wing on the driver’s side. There was also some rust damage here too. (Click on images for full resolution.)

Collision and rust damage
I decided to first attack the rust at the rear of the arch and below the seam.I marked out what I thought to be a generous cut into sound material and fabricated a patch panel. This is a fairly complicated panel since it has compound curvature and curved/folded seams on two edges. But it came out fairly well forming it over a variety of blocks. Without having a shrinker/stretcher I made the seam flange follow the body curve by peening the outer edge to stretch it.

Under quarter panel
I was actually pretty happy with this until I melted out the lead in the area. I had been hesitant to do that until I had the patch panel correctly formed since a lot of the curvature I was trying to match was formed with lead. When the lead ran out I discovered massive rust damage hiding beneath. So either someone long ago used lead to cover up a rust through or the rust formed under the lead. With the amount of distorted metal in the rusted area I’m thinking the former although I suppose it’s possible the factory leaded over some construction damage. Either way the patch panel I was so proud of was now too small and probably scrap. Dead end number one.

Rust hiding under lead. Patch panel only covers 75% of it.
So on to the collision damage. Cutting out the rusted areas gave me partial access to the dents but to get fully behind the damage with a dolly, I had to cut some major portions out of the inner wing too. You can also see how much larger the under quarter patch panel needs to be to eliminate the rust revealed by melting out the lead (dashed lines).

Prelim cutouts for patch panels

Inner fender well cut away to get behind damage
With the dent pounded out reasonably well, I decided to work on a patch panel for the wing. I didn’t get too far before I realized this panel can’t be installed until after the sill has been replaced since it covers the sill joint. Dead end number 2.

Wing covers this seam--sill has to be done first
OK, so the time has finally come to cut out the complete sill. The scale and risk of that job had intimidated me for quite awhile. I began to be concerned with the strength of the car once the sill was out (and the floor pan insert not yet replaced). To see if there was merit to this fear I re-installed the hinges and doors and checked the B-pillar gap with the body upright and then inverted on the rotisserie. The change was substantial but a lot of it was due to wear in the driver side hinge. This allowed the door to move up and down accentuating the gap. Fortunately the passenger hinge was still very tight, giving me a more accurate picture of the body deflection—about 1/8” difference in door gap–due primarily to body flex. This would only get worse with the sill removed so I decided to build some reinforcement struts. Not quite dead end number 3 but certainly a left turn I hadn’t counted on.
To properly position the struts I needed set the door gap correctly and then nail down the struts. Except the driver hinge was so bad I couldn’t gap the door. So the hinges needed to be rebuilt first. Another left turn. Remember I’m only trying to replace the sill so I can fix the wing and match it with the repaired arch (after I remake that panel). I’m beginning to think I have autobody ADD.
With the help of Harvey Ferris’ excellent instructions, I rebuilt both hinges. The only departure I made was using a 0.499 dia undersize reamer instead of the adjustable reamer. Apparently ENCO had a bad run of them and refunded my money after sending me two units. It’s too bad they couldn’t source a quality unit but they were very good about a full refund including the shipping on the two units. I would do business with them again. Anyway, the reamer (from McMaster) worked very well and the hinges came out very well. You just have to carefully mic the rods before deciding what size reamer to buy. Running a 31/64” drill through the bores left just enough for the reamer to clean up beautifully leaving a good ringing fit.

Drill and ream hinges

New 1/2" pins fitted to brackets
With fresh hinges the doors could be aligned and the struts installed. It now passed the inversion test just fine.

Struts in place
I’m not sure why, maybe it was my lingering intimidation of the sills but I decided to repair the doors while I had them handy. Also, the passenger door had some rust on the bottom edge that would require a patch panel to be fabricated. I wanted to have that door correct before I pulled the sill since I planned to realign the new sill with the door. It was about this time that I realized the car is built around the doors. Once the door is in place, the B pillar shut face, the sill and the bulkhead side panel (which forms the A pillar) all need to line up. More reason to the get the doors right before going any further. So, another left turn, but at least one of my choosing.
Cutting out the rust and making a patch panel for the lower door was straight forward with the help of the Tin Man video “Autobody Steel Patch Panels”. Here’s the panel ready to go.

Joggled door bottom patch panel
I also had some rust perforation at the top of the door where there is a built water trap on Series 1 cars. So I cut out the bad area and formed up a rather tricky patch panel (at least for me). It came out well, life was good.

Upper door perforation

Bad area cut out

Patch panel in place
Before I welded in the two panels I decided to give the door a sodium gluconate electrolytic bath to leach out any hidden rust in the seam above my repair. After the treatment, I opened some of the seam and was appalled to find extensive hidden rust.

Rust inside seam
The door would have to be reskinned and the considerable patch panel work would be thrown out. This counts as a bonafide dead end. Number 3 I think.
I ordered a new skin from SNG and while waiting for it proceeded to the other door which turned out be completely sound. With its rebuilt hinge, the alignment was good so I was finally able to cut out the sill and the bulkhead side cover.

Sill and side cover removed
With the sill removed, it was finally time to install the floor pan insert. I had held off on this as long as possible because it improves the access for blasting, painting and hinge adjustment. SNG floor pan inserts are now shipped with a tough powder coat finish. This was ground off in the joint area and Weld Through primer applied before welding. So with the help of the world’s largest sliding bar clamp (another left turn but really really helpful), I perimeter welded the new floor. This had to be done before the new sill could be installed since the sill joint overlaps the floor pan joint.

Floor pan welding with help of long reach clamp

Floor pan welded and ground
Pretty decent weld penetration too. But the fumes from the burning powder coat and WT primer in the joint are pretty nasty. Good ventilation and a mask are a must.

View from inside foot well
Fitting the new sill was trickier than I thought it would be. It was far from an exact match, so you just had to choose what set of compromises you were willing to make. In the process of doing that, I completely ruined it beyond repair. Dead end number 4. A new sill from SNG arrived the next day so I got to try again—this time with experience. I believe I’m also invited to the SNG Christmas party.
The fit up went better this time but not having spot welder I had to punch about 200 plug weld holes. Then I blasted the cavity and painted it with self etching primer and applied CRC heavy duty rust preventative. I masked the joints and then applied weld thorough primer to the lapped areas. Joint clamping courtesy of the big clamp again.

Media blasted with aluminum oxide

Prepped and ready to weld

Door opening seam aligned and clamped

Floor edge clamped
After what seemed like an eternity of welding and grinding, one sill is in.



And that brings us up to date. It’s been exactly a year since I started stripping out the interior. I guess that formally ends my estimate of finishing in a year!
Next on the list, re-skinning that door.